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Tractorsport Flowbench Forum Archive • View topic - 200 CFM Research

200 CFM Research

Share whatca have found? Brainstorming? Only open to members

Postby 106-1194218389 » Mon Nov 03, 2008 11:26 pm

Tom,
Another thing you could do on the head you cut up is just drill a 1/4" hole in the bulge in a couple of places to see how thick it is and then port the test head that is cut up and just put clay in the holes when you flow test.
John
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Postby Otto » Tue Nov 04, 2008 1:37 am

i agree that right side bulge is not helping drill and clay like john say's we are talking sand casting's they could just as easily be solid there and looks to be creating a secondary pinch with the the dogleg and reducing bowl volume i looks lke it needs to darn near straight from the casting seam at about 1:30 to about 3:00 or just past inthe bottom photo but I'm a bike guy
Otto

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workin to play
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Postby larrycavan » Tue Nov 04, 2008 7:11 am

I just cruised the last couple pages real quick so I'm not fully up to speed at the moment....

The turbulence IMO is being caused to a large degree by the too rapid expansion of the port. I see this all the time in certain heads I do because they are both bent and shaped for swirl.

Get some clay, go in there and fill in that section prior to where your pencil is pointing and things should calm down. Clay will show you a great deal about what works and what doesn't for picking up CFM. Curved ports are a mother when you start giving them bowl volume on the fast [curved] side. Things get off balance real quick....
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Postby 106-1194218389 » Tue Nov 04, 2008 1:39 pm

I tried to find photos that would show what the early Vortec heads were like as they had a ramp in them. All the Vortec head pictures I find now are the new style which is similar to a regular SBC head - Sorry I tried. AMC had a similiar head on the intake if I remember correctly.

John
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Postby 49-1183904562 » Tue Nov 04, 2008 3:51 pm

Tom,

Go to the Depot and in the electrical section they sell a clay that is for sealing arond open wires, Made by GB products and comes in a 8 X 2 X 1 bar. It is oil based sticks well and will stay soft for years. I also use the same clay for checking Valve to piston clearance.

Rick
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Postby larrycavan » Tue Nov 04, 2008 8:53 pm

If this is a test head, here's what I'd try.

Between the yellow arrows, loose all that casting slag. Get a better radius shape to the bowl. Get back under the seat as much as you can. Radius right on around so the front of the bowl has a radius under the seat as well. I've picked up a bunch of flow using that method before.

On the right, fill with clay, the section in grey. Also, there's a bunch of low spots and waves in that beveled portion of the bowl. Clean that up and radius over that straight up wall better. Loose as much of that wall as you can.

Blitz that ramp on the right side of the guide and get some more area there in the roof.....

Anyway...those are the things I'd do if that was a test head.




Edited By larrycavan on 1225846733
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Postby 200cfm » Tue Nov 04, 2008 10:15 pm

Ok, that gives me some guidance. These are the heads going on the 330. The last time I used them was back in 06 season and spring of 07 when this motor was in the yellow Lark. They have about 75 quarter passes on them and I had done some chamber work on them but no porting into the port itself until this fall. They were averaging around 160-165 cfm with the larger (1.850) valve and the chamber work. With this falls port work they are averaging 170 to 175 cfm. So the clean up and extra CSA (not much really removed) has helped.

Take a view of the following photos that I took prior to this falls work. These are the patterns I notice on every intake valve removed. This photo is number 1 which had some oiling issues from the exhaust guide. But the above #5 port had the same patterns only reversed directions because the port turn is in the opposite direction. I see it as a engine running wet flow test photo. I marked the areas of interest to orient the valve for study.

Image

Here is the valve flow pattern when oriented to the marks. Note the clean area which I interpret as fuel wash or fuel fall out. And on the very opposite side are carbon trail deposits which I interpret as reverse flow.

Image


Another view. Just imagine it rolling over into the guide on install and you have the orientation.

Image

Better view of the area of interest. This area corresponds to the chamber shroud side which corresponds to the above bowl area that Larry marked.

Image

And that same side has this mark up near the top of the stem. A wash area I call it.

Image

And a view of the opposite stem side facing the exhaust, no wash on the stem.

Image

I won't have the time to test all the recommendations on these heads but will hold those suggestions for the "red head".
I want to get them back on the short block and make a install before the track closes by Thanksgiving. Hopefully I can get the rings seated, and get the motor broke in, etc. I am simply running out of time to do every thing. I am practicing 30 degree backcut grinding on the valve refacer and want to make that addition to all the above valves before I put it together.

tom
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Postby blaktopr » Wed Nov 05, 2008 12:17 am

Here is my take from testing and my mouse is crap! As you read this, look at the black areas as fuel puddleing and not being burned thoroughly leaving the sooty black residue. The cleaner spots, had higher speeds keeping some fuel more suspended, until a radical speed increase, dropping the fuel out. I tried to illustrate the pic. Blue lines airflow. Red lines, faster airflow. Magenta, even faster around plug. Yellow is fuel. The three yellow lines on lower right hand corner leading to the quench pad would be under turbulent conditions with larger droplet size congregateing on the wall below it. I am only speculating this without testing your head, but referencing to mine, so don't kill me. The black spot between the two valves and below the plug is where the fuel vortex is and is loose fuel. Burned slower with less O2, so black. Clean ring across plug where speed of air and fuel matched out of seat area, more burned uniformly. Dark area over that clean ring, speeds fast out of seat driving some fuel to ram in and pile up a little then being pushed around toward the exhaust but unable to be drawn back into the fast airstream so just stays there as a thinish layer. Same goes for under the intake toward the exhaust. ( I am referencing top/bottom to the pic only.) The two paths meet on the cylinder wall. Some of the blacking on the exhaust valve, fuel just slowly trapped and moving around in a circular pattern and side to side. Black at the edge of the exhaust valve same side of intake, (no yellow, sorry) fuel separating as speeds increase across the margin. Yellow dots around intake valve, fuel droplets stuck to the edge of the seat cut and margin. Dark area around intake at chamber wall over cylinder wall, same high airspeed, fuel separation as other spots of chamber. Most chambers are smooth, yet to combat some separation problems in the runner, we make it very course. The chamber is treating the fuel as if you polished the intake runner.

As for the spot on the valve inside the runner, over the severe dogleg, That I think is there because at the higher airspeeds not only does air not want to make that sharp turn, but also the fuel. So both tends to follow the straightest path to the valve and not even touching that section of the valve. If any fuel separates to behind that buldge and forms on the walls, the airspeed is too slow back there and the high pressure area pushes it down along the wall utilizing only the seat and not the face of the valve, therefore not touching that part to leave any fuel and depositing it in that area in the chamber on the wall side.(I think I have the port bias right) Leaving the black deposit. Just trying to contribute.
Chris
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Postby blaktopr » Wed Nov 05, 2008 12:32 am

Just want to add now myself looking and reading. Concave bowl on exhaust with angles leading to margin I see. Not only does the dark ring closest to intake valve have fuel separating there, as air/fuel crosses over margin and the angles leading to the "bowl" of the valve, the same conditions happen as does over the plug. After the fuel drops out it stays in that void. I guess that it takes less work to reside on the surface of the valve than to re-enter into a fast moving airstream running across the face of it. I know that should be an area of higher pressure, but it must be the same as throwing a plastic bag into the spray of a garden sprayer or why when you try to flick a cigarette butt out an open window, but just ends up coming back and landing in the back seat. :D
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Postby 200cfm » Wed Nov 05, 2008 10:47 am

Thanks Chris for the chamber readings. The best I got out of those heads as you see them was 13.37 @ 101 in the stude Lark. Here is an early testing.

Image

And once I got things sorted out better with the car. It was not a killer off the line.

This is an interesting photo back from the summer of 06.

Image

I matched up Pipemax data based on Effective Ve% using my bench port flow data of around 165 cfm port radius minus the 16% factory intake manifold loses (net around 136.6 to 143.4 cfm) and Pipemax calculates the hp at 271.1 Low side. When checked in HP from ET slip it hit the photo data run nearly dead on. Love and trust that Pipemax.

Plus the ET for Analyst hit it dead on too. Amazing!

60 ft : 1.914
330: 5.574
660: 8.619 @ 80.060
1000: 11.275
1320: 13.514 @ 100.83

Image
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Postby blaktopr » Wed Nov 05, 2008 3:12 pm

Wow Tom, you don't see that everyday! Glad to see you are able to make the out of the ordinary work well. Man, that car can make some guys cry on the street. I wonder if anyone can chime in on my readings letting me know what I may be missing to continue learning. Plus I don't want to steer anyone in the wrong direction.

Chris.
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Postby 106-1194218389 » Wed Nov 05, 2008 3:21 pm

Tom,
do you still have that Lark? That is a cool car. I always loved those - I had a friend that had a supercharged version that was a black 2dr hardtop with a 4 speed.
John
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Postby larrycavan » Wed Nov 05, 2008 6:41 pm

Which Ve calc method did you use in PipeMax?
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Postby 200cfm » Wed Nov 05, 2008 9:28 pm

Yes, I still have it. Parked and needing attention. New import paint is starting to fade on the roof though. I put another motor in it to move it around and out of the way here.
Here is a view of that 330 when it was installed. That's my DIY paint job and ebay win bid graphics work.

Image

Image

Image

Larry, I used the drop down menu Estimate Ve%. John says you are suspose to use the 3 entries from that drop down if you know the lost from flowing the manifold. My new efficency net came in at 87.9%. Before I used 100% which set the cfm in Pipemax to where my heads flowed (avg) if the data was from head port only.

I had a good day on the bench and the grinder today. I did some more practice grinding and made my first 30 degree backcuts. Did some flowing and I must say, this backcut is a blessing in helping the numbers. I thought the bench was acting up but repeats and other port flows showed similiar gains. I have come to really appreciate a 30 degree backcut. Will host up some data later. Haven't done any stone grinding yet.

tom
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Postby 200cfm » Fri Nov 07, 2008 11:28 pm

Finished up the heads for now and they are ready for install on the short block. Very pleased with the gains. Took much longer than I anticipated (over 4 weeks) but if I don't stop now I want have time to track test before the season shuts down. I applied a 30 degree backcut to all the intakes and the exhaust with the B & D valve refacer. Used the old stone pending the arrival of the Goodson stones. Didn't touch up the 45 part in the head or the valve. Just lapped those parts together. On speed tallk the don't like lapping but that's all I have used in the past.

Now on this 30 cut, I was surprised and pleased at how so little a cut or angle could have such an influence on the flow numbers. I flowed several ports with the 30 cut and they all posted gains. Very evident from the incline rise values on each lift. Only the .100 lift offered no significant change, but the others took off nicely. This will be my first set of heads with a backcut. The backcut also helped the exhaust numbers. So both were a win/win. Here is data on one of the best ports.

Port 4 (45) Port 4 (45 + 30 backcut)
LIFT CFM CFM gain
0.100 60.3 60.5 0.2
0.200 101.5 109.8 8.3
0.300 138.7 149.8 11.1
0.350 155.5 163 7.5
0.400 165.9 171.5 5.6
0.450 174.8 178 3.2
0.500 178.6 181.2 2.6
0.525 178.8 181.6 2.8

Here is a before and after of the above valve after cleanup.

Image

Image
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