by Dom G » Wed Dec 14, 2005 7:55 pm
Thanks for the continuing support and ideas everyone, I appreciate it.
I'm going to try to respond to Larry, Mouse and Mousehouse1 since each of you commented or made suggestions to my last post.
I'll respond to Larry last since I made the changes he suggested and the results may mean something to you guys, but not to me at this point.
Mousehouse1
Yes, I have 6 motors presently. Since I've been struggling with testing up to this point I can't honestly say what the total cfm I've been able to pull. If the testing that suggests one of my orifice ranges is really accurate I know I can pull about 160 cfm with 4 motors. I may find I'll need to make many of the changes you made to get my bench straightened out. Since we are both using the same motors, I'm wondering how many motors you need to turn on when doing a leakage test @ 28"? I have to use 4.
Mouse
To answer your question about the nearest supporting structure or material I attached a picture I took when I was making the change Larry suggested. The two pressure fingers are about 7/8" high and 2 1/2"-3" away from each side of the orifice. Also the back wall is not too far away from the top of the orifice.
Larry
It takes 4 motors to pull 28" with the calibration plate and the 2" orifice.
You had mentioned to check my T fitting to make sure it wasn't cracked or leaking. Since I'm not using a T fitting a light went on in my head and said to reroute your vertical manometer pickup from the head adapter, where I actually have had it connected, to the probe running to the upper plenum to see if I get the same readings.
With the intake control valve in the same position using the calibration plate and 4 motors, I obtained the same 28" reading. I tried it again with a tee in the line as well and the reading was the same again. I'm not sure if this has any significance?
Next, I made the changes you suggested. I selected the 2.531" orifice. I covered 1/2 of it with a piece of metal and duct taped it in place. I also duct taped all other orifices and around the sealing ring so air could only theoretically pass through one half of the 2.531" orifice.
When you said to leave everything else in place, I assumed you meant leaving the calibration plate in place as well so I did.
Now the drum roll and the results.
With 4 motors on, I could only get to 20" of pressure when the inclined manometer got to 100%. I had to close down the control valve a bit to keep the inclined from going over 100%.
By the way, if you notice from one of the pictures I attached, I offset the hole in the benchtop from the orifice to avoid having a straight line.
So what do these results tell us and where do I go from here?